Analisa Koordinasi Proteksi Feeder Lakarsantri pada Transformator II 50 MVA GIS Karangpilang

Authors

  • Reza Sarwo Widagdo Universitas 17 Agustus1945 Surabaya
  • Gatut Budiono Universitas 17 Agustus1945 Surabaya
  • Hadi Tasmono Universitas 17 Agustus1945 Surabaya

DOI:

https://doi.org/10.56795/fortech.v2i2.206

Keywords:

Over Current Rele, Protection Coordination, Short Circuit

Abstract

In the event of a short circuit interruption it is still very worrying where there are still many problems with protection equipment that does not work properly. In field conditions, the transformer at GIS Karangpilang often fails to disconnect the feeder. Based on this incident, it will be discussed how to coordinate the relay between incoming and Lakarsantri feeders. The calculation results from the working time of the relay feeder are 0.3 seconds with the working time on the incoming part being 0.68 seconds. Based on data from GIS Karangpilang, the working time of the relay in the feeder section was 0.41 seconds and 0.69 seconds in the incoming section with a fault current of 4.5 kA showing good results. In the short circuit simulation results, the manual calculation data and the data obtained from the Karangpilang GIS are not much different, where the working time of the relay feeder is 0.11 seconds faster than the incoming working time, with a time of 0.7 seconds which is in accordance with the relay settings.

 

Author Biographies

Reza Sarwo Widagdo, Universitas 17 Agustus1945 Surabaya

 

 

Gatut Budiono, Universitas 17 Agustus1945 Surabaya

 

 

 

Hadi Tasmono, Universitas 17 Agustus1945 Surabaya

 

 

 

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Published

2021-09-23

How to Cite

Sarwo Widagdo, R. ., Budiono, G. ., & Tasmono, H. . (2021). Analisa Koordinasi Proteksi Feeder Lakarsantri pada Transformator II 50 MVA GIS Karangpilang. Jurnal FORTECH, 2(2), 69–75. https://doi.org/10.56795/fortech.v2i2.206